by model murdering » Fri May 24, 2019 10:28 pm
Hi Scott,
I have pix somewhere.
I did a pair of black AW Studes waaaaay back when in the HT dayz for the charity auctions. Mostly for giggles. It's kinda blurry; but it suffices to say that one thing led to another. I bushed the rear axle, then the armature and driven gear holes in the gear plate, and the armature hole in in the comm pit. Along the way, I changed all the gears to t-jet style, dropped to a nine tooth, eventually scrapped the rotten toothed early crown gear, the play-dough axles, and switched to Thunderbrushes instead of the dumbed ... er ... domed brushes, because they dont "cant" and bind in the guides.
Obviously everything was hand fit. The AW plastic is pretty gooshy and will move a lot if you press in something with too chubby of an OD for the selected bore size. I spun my bushing stock down in the dremel with a file and 320 paper to help ease the plastic distortion, but still keep a good impinge fit. I also champfered the leading side of bushing and smoothed it on some 600, to help them glide in when pressed. I used my RTHO presses, and what I couldnt wrangle with those; I used my small mini drill press.
You'll have to size a drill blank or what have you, to suit your chosen rear axle bushing stock. The differential between OD of the AW axle spline and the smooth journal portion is great enough that by the time you get your new bushing over the spline hump, the slop quotient wont be spectacularly improved when you drop back onto the journal.
At the time I was goofing around with this, one of the main issues was that the armature shaft and the pinion shaft werent vertically parallel to one another when the gear plate and the chassis were together. Generally, the arm was leaned back towards the idler, and the pinion bore in the chassis tail plate has to move back a skoshe. Honestly, I never bothered to see if I could get a better fit by mixing and matching components, like you would with a T-jet build.
You have to leave the armature hole in the chassis pit where it is. There really isnt a whole lot of room to work with. Spacing here is critical. The OD of the bushing cant be so great that pressing it in distorts the edge of the brush guide holes where they face the shaft (center). Some AW chassis arent particularly forgiving with the brush to guide clearance, so ya gotta watch it. If you bone it, you can shave the offending curl off the bore with a fresh #11 blade and a minimum of caffiene.
For the gear plate, I flute reamed the armature hole using my pinvise, concentrating my efforts to push the bore forward (back towards plumb). Then I re-bored the hole a shade over and pressed the bushing in. The result was that the armature gear now addresses the idler gear properly (level). The rub is that it pulls the gear centers apart, fractionally. Regardless, it loosened the drive train up nicely. I left the cluster gear bore as is, over-bored slightly, and just pressed the insert. Same flute ream trick for the tail plate bore where the pinion shaft drops in, but instead of moving forward towards the guide like the armature hole, you push it back ward towards the rear screw post.
All in all, the whole enchilada wasnt so jerky and weirdly stiff anymore, such that they were. Even with the grabbier magnets, the coast-fly-wheel effect was much improved, with smooth acceleration and deceleration. The brass bushings will be more thirsty than the conventional arrangement. Like a big scale slot they'll talk and clatter at you when oiling is required. In the end, I threw a lot of parts and effort at it for the halibut. I still think the best bang for the buck tweak for the JLTO, is to re-arch the shoe hook and take about 87 tons of excess pressure out.